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The Jin Zhong Pulp and Paper Mill, Hefei, Anhui Province

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Description

Jin Zhong paper mill is located in Hefei (the capital of Anhui province). It was established in 1978. It presently has a workforce of 820 workers, including 48 persons having a technical background. Its annual production capacity is 75 000 tonnes. The mill operates eight paper machines producing low, medium, and high quality cardboard. The main raw material used at the mill is waste cardboard. Depending upon the level of quality targeted, some market softwood pulp is also used in the process. Fresh water entering the process comes from South Wee river and wastewater is discharged to the Er Shi Pu river. Jin Zhong paper mill mainly sells its products across Anhui province and to packaging plants located in neighbouring eastern provinces.

The following information about the mill's Cleaner Production activities is drawn from the January 2001 evaluation - Assessment of the CP Solutions in the Pulp and Paper Sector, April 2001. More details about these solutions are available in the full assessment document, which is available in downloadable format. The factory receives assistance in implementing cleaner production from the China-Canada Cooperation Project on Cleaner Production.

Wastewater Treatment Facility

Jin Zhong mill is equipped with a wastewater treatment plant having a design capacity of 200 to 250 m3 per hour. It consists of a series of inclined screens followed by a settling tank and a primary clarifier. The treated effluent is discharged to a channel going to the Er Shi Pu river. The treated effluent is monitored for COD, SS, and pH by the local Environmental Protection Bureau (EPB) since the mill does not possess its own environmental monitoring laboratory. In general, the mill complies with the national standards except for COD which slightly exceeds the compliance level.

Cleaner Production Solutions

Jin Zhong paper mill has implemented twenty CP solutions. Out of these twenty solutions, three are no cost solutions, twelve are low cost, four are medium cost, and one is high cost.

CP Solution Number

Implemented CP solution

Category of Solution

1

Raw material (waste cardboard) sorting

No cost

2

Good housekeeping procedures

No cost

3

Process optimization

No cost

4

Coal blocks are now crushed to smaller size. Jin Zhong set up its own standard for coal.

No/low cost

5

Installation of a filter at the water inlet to prevent clogging

Low cost

6

Installation of two cyclone dust removal

Low cost

7

Reduction of consumption quotas pertaining to coal, electricity, and additives.

Low cost

8

White water recycling to the raw material feeder instead of using fresh water.

Low cost

9

Employees training – environmental protection awareness sessions and sessions pertaining to operations.

Low cost

10

Trimming of the paper roll is carefully monitored

Low cost

11

Training sessions for the managers

Low cost

12

Equipment maintenance

Low cost

13

Ashes from boilers are now sold to brick manufacturers

Low cost

14

Use of antiwear on compressors allowed to decrease the production cost by 3 yuan per ton of paper produced.

Low cost

15

Water from the vacuum pump is reused for paper roll trimming

Low cost

16

Addition of 10% talc to the pulp in workshop #7 & #8

Medium cost

17

Fibre recovery from the wastewater

Medium cost

18

Set up of a flotation unit allows to treat 50 000 tons of wastewater per year compared to 20 000 tons per year before the construction of this unit

Medium cost

19

Insulation of the steam pipes (5% energy consumption reduction)

Medium cost

20

Boilers replacement 10% energy saving

High cost

The Jin Zhong mill has established a CP program which is well balanced between management issues and manufacturing issues. The CP solutions that were implemented so far are numerous and diversified. This indicates that the various departments of the mill have been significantly involved. 

The mill established ambitious environmental targets. Before the end of year 2001, the mill is planning to proceed with the implementation of some low to high cost solutions. The implementation of these future CP solutions are expected to lead to a further 3% reduction in raw material consumption as well as a 10% reduction of energy consumption.

 

This picture shows that recycled white water is now the only type of water that is used in the raw material feeder. Previously, there were two water lines in the vicinity of the feeders – one line was fresh water and the other was recycled white water. Now, only the recycled white water line can be used by the workers; the fresh water line is no longer available in order to ensure that only recycled white water is used at this stage. (CP Solution #8)

 

This picture shows that steam pipes have been insulated. This medium cost solution leads to an energy consumption decrease. (CP Solution #19)

 

The residues generated by the boiler used to be wasted. These residues are now recuperated and sold to brick manufacturers. (CP Solution #13)

 

Two cyclone dust removal systems were installed next to the boiler room, which collect dust generated by the boilers. (CP Solution #6)

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Contact 

The factory can be contacted by email at e-mail: hfjzzy@mail.hf.ah.cn  

Contact Name: Mr. Pen Yuanfung (General Manager) 
Address: Hefei, Anhui 
Phone number:(551) 453-4116
Fax: (551) 453-2820
Email:
hfjzzy@mail.hf.ah.cn
Web Page: none

Links

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